D9001 - 1969
January
| 1 - | |
| 2 - | Finsbury Park TMD. Boiler J2942 on test - results: satisfactory for service age (fitted 29.03.68). Notes: "No visible makers number on shell plate or Mobrey housing flange." One report wrongly identifies boiler as J2952. |
| 3 - | |
| 4 - | |
| s5 - | |
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| 7 - | |
| 8 - | |
| 9 - | |
| 10 - | |
| 11 - | |
| s12 - | 1N16 13:20 King's Cross - Bradford. |
| 13 - | |
| 14 - | 1N01 22:45 King's Cross - Bradford, to Leeds. |
| 15 - | |
| 16 - | |
| 17 - | |
| 18 - | 1A48 17:05 King's Cross - Newcastle. |
| s19 - | |
| 20 - | |
| 21 - | |
| 22 - | |
| 23 - | |
| 24 - | 1A17 08:00 Edinburgh - King's Cross. 1N22 16:20 King's Cross - Bradford. |
| 25 - | 1A21 11:00 Newcastle - King's Cross. 1A60 19:40 King's Cross - Aberdeen, "The Aberdonian" to Edinburgh. |
| s26 - | |
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February
| 1 - | |
| s2 - | |
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| 5 - | |
| 6 - | |
| 7 - | |
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| s9 - | |
| 10 - | |
| 11 - |
Casualty report card states: Boiler defective - water tank almost
empty (tank filled). 42,000 miles since last classified repair (22.11.68). |
| 12 - | |
| 13 - | |
| 14 - | |
| 15 - | |
| s16 - | |
| 17 - |
Casualty report card states: Flashover on No.2 main generator - no
apparent cause (damage cleaned up). 42,600 miles since last classified repair (22.11.68). |
| 18 - | Finsbury Park TMD. Boiler J2942 on test - results: Gas analysis Co2 test satisfactory (fitted 29.03.68). |
| 19 - | |
| 20 - | |
| 21 - | |
| 22 - | |
| s23 - | 1N16 13:20 King's Cross - Bradford. |
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| 28 - |
March
| 1 - | 1A37 10:30 Aberdeen - King's Cross, from Edinburgh. |
| s2 - | |
| 3 - | |
| 4 - | |
| 5 - | |
| 6 - |
Casualty report card states: Short of boiler water - scoop damaged
(scoop repaired). 54,000 miles since last classified repair (22.11.68). |
| 7 - | |
| 8 - | Finsbury Park TMD. Shopping proposal dated 24.04.69 suggest loco off 1500-1800 hrs exam. |
| s9 - | |
| 10 - | |
| 11 - | |
| 12 - | |
| 13 - | 1A26 12:00 King's Cross - Aberdeen, to Edinburgh. |
| 14 - | |
| 15 - | |
| s16 - | 1A47 09:30 Aberdeen - King's Cross, from Edinburgh |
| 17 - |
Casualty report card states: boiler failure - burner motor fuse
blown (fuse renewed). 57,000 miles since last classified repair (22.11.68). |
| 18 - | |
| 19 - | |
| 20 - | |
| 21 - |
Casualty report card states: Boiler defective - Mobrey chamber
blocked (chamber cleaned out). 61,000 miles since last classified repair (22.11.68). |
| 22 - | |
| s23 - | |
| 24 - | |
| 25 - | 1E83 16:20 Harrogate - King's Cross, from Leeds. |
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| s30 - | |
| 31 - |
April
| 1 - | |
| 2 - | 1A05 07:50 Newcastle - King's Cross. King's Cross Loco. |
| 3 - | |
| 4 - | Good Friday - Sunday service only. |
| 5 - | 1A31 12:00 Edinburgh - King's Cross. |
| s6 - | |
| 7 - | |
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| 11 - | |
| 12 - | |
| s13 - | |
| 14 - | |
| 15 - | Finsbury Park TMD. Boiler J2942 on test - results: Chemical dosage equipment to be overhauled & recommend boiler be acid washed. |
| 16 - | Finsbury Park TMD. boiler repairs. |
| 17 - | Finsbury Park TMD. Boiler J2942 on test - results: Satisfactory for service. |
| 18 - | Finsbury Park TMD. Shopping proposal dated 24.04.69 suggest loco off 500-600 hrs exam. |
| 19 - | |
| s20 - | |
| 21 - | Casualty report card states: Short of
boiler water - waterscoop mouthpiece set too high (mouthpiece set to gauge). 78,600 miles since last classified repair (22.11.68). |
| 22 - | |
| 23 - | |
| 24 - | Peterborough TMD. Taken out of service - for works attention Casualty report card states: No.2 engine piston through crankcase - loco TOT. 81,000 miles since last classified repair (22.11.68). |
| 25 - | To Doncaster Works - Unclassified repair. No.2 power unit 408 con rod through crankcase - 408 replaced by 439. 80,820 miles since last classified repair. |
| 26 - | Doncaster Works. |
| s27 - | Doncaster Works. |
| 28 - | Doncaster Works. |
| 29 - | Released from Doncaster Works. |
| 30 - |
May
| 1 - | |
| 2 - | |
| 3 - | |
| s4 - | |
| 5 - | New timetable period |
| 6 - | |
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| 10 - | |
| s11 - | |
| 12 - | Casualty report card states: Loss of power
- GC32 operating coil not energising (P43 wire & terminal refitted). 84,000 miles since last classified repair (22.11.68). |
| 13 - | |
| 14 - | Finsbury Park TMD. Taken out of traffic - awaiting works attention. |
| 15 - | |
| 16 - | To Doncaster Works - Unclassified repair. Shopping proposal states: No.6 traction motor on No.2 bogie 9000-28 earth defect - No.6 traction motor was replaced. 88,000 miles since last classified repair (22.11.68). Released from Doncaster Works. |
| 17 - | 1A01 07:25 Lincoln - King's Cross, from Peterborough (ex D1874). |
| s18 - | |
| 19 - | |
| 20 - | |
| 21 - | |
| 22 - | Casualty report card states: Loss of power
- boiler water required - scoop defective. 93,000 miles since last classified repair (22.11.68). 1S32 12:00 King's Cross - Aberdeen, to Edinburgh. |
| 23 - | |
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| s25 - | |
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| 28 - | Shopping proposal: Due Intermediate Repair. 1L22 15:55 King's Cross - Harrogate, to Leeds. |
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| 31 - |
June
| s1 - | Casualty report card states: Flashover on
all machines - not determined (0400 insulator removed). 94,000 miles since last classified repair (22.11.68). |
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| 14 - | 1A12 08:10 Newcastle - King's Cross. |
| s15 - | (1A33 11:30 Newcastle - King's Cross). |
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| s22 - | 1L16 13:20 King’s Cross - Bradford. |
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| s29 - | |
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July
| 1 - | |
| 2 - | To Doncaster Works - Intermediate
repair (due 28.05.69). Shopping proposal states: No.1 power unit 438 time expired 112,410 miles since last classified repair (22.11.68). Power units No.1 438 replaced by 454 & No.2 439 replaced by 428, bogies No.1 9000-27 replaced by 9000-3 & No.2 9000-28 replaced by 9000-4 and boiler 1486/J2942 replaced by 1494/J2950. The body was given an Intermediate repair and repainted into blue livery with full yellow ends - the 'D' prefix is most likely to have been dropped from the number at this time. |
| 3 - | Doncaster Works. |
| 4 - | Doncaster Works. |
| 5 - | Doncaster Works. |
| s6 - | Doncaster Works. |
| 7 - | Doncaster Works. |
| 8 - | Doncaster Works. |
| 9 - | Doncaster Works. |
| 10 - | Doncaster Works. |
| 11 - | Doncaster Works. |
| 12 - | Doncaster Works. |
| s13 - | Doncaster Works. |
| 14 - | Doncaster Works. |
| 15 - | Doncaster Works. |
| 16 - | Doncaster Works. |
| 17 - | Doncaster Works. |
| 18 - | Doncaster Works. |
| 19 - | Doncaster Works. |
| s20 - | Doncaster Works. |
| 21 - | Doncaster Works. |
| 22 - | Doncaster Works. |
| 23 - | Doncaster Works. |
| 24 - | Doncaster Works. |
| 25 - | Doncaster Works. |
| 26 - | Released from Doncaster Works. |
| s27 - | |
| 28 - | |
| 29 - | |
| 30 - | |
| 31 - | 1S17 10:00 King's Cross - Edinburgh "The Flying
Scotsman. To ? as Finsbury Park issue following shopping proposal & low miles. Finsbury Park shopping proposal: flashover damage. Miles since last classified repair 500 (26.07.69). |
August
| 1 - | To Doncaster Works - Rectification. Shopping proposal states: Flashover damage on both main generators and slight flashover damage to all traction motors on No.1 bogie 9000-3, No.2 bogie 9000-4 had slight flashover damage to No.s 4 & 5 traction motors whilst No.6 traction motor needed one brush renewing - all flashover damage was repaired. 500 miles since last classified repair (26.07.69). |
| 2 - | Doncaster Works. |
| s3 - | Doncaster Works. |
| 4 - | Doncaster Works. |
| 5 - | Released from Doncaster Works. 1S35 14:00 King's Cross - Edinburgh. |
| 6 - | |
| 7 - | 1L16 13:20 King’s Cross - Bradford |
| 8 - | |
| 9 - | |
| s10 - | |
| 11 - | |
| 12 - | 1A15 09:15 Newcastle - King’s Cross, "The Tees-Tyne Pullman". |
| 13 - | |
| 14 - | |
| 15 - | |
| 16 - | 1L33 17:05 King's Cross - Bradford. |
| s17 - | |
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| 23 - | 1S20 10:10 King's Cross - Edinburgh. |
| s24 - | |
| 25 - | 1A12 08:10 Newcastle - King's Cross. |
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| 27 - | |
| 28 - | |
| 29 - | 1N10 11:00 King's Cross - Newcastle. |
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| s31 - |
September
| 1 - | |
| 2 - | |
| 3 - | |
| 4 - | |
| 5 - | 1D18 19:00 King's Cross - Cleethorpes. |
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| 19 - | Finsbury Park TMD. Brake & battery test. |
| 20 - | |
| s21 - | |
| 22 - | 1N27 18:00 King’s Cross - Newcastle. |
| 23 - | |
| 24 - | |
| 25 - | |
| 26 - | 1A04 07:30 Leeds - King's Cross. 1S35 14:00 King's Cross - Edinburgh. |
| 27 - | 1L13 11:52 King's Cross - Harrogate. 1A33 17:20 Bradford - King's Cross. |
| s28 - | |
| 29 - | 1N10 11:00 King's Cross - Newcastle. |
| 30 - |
October
| 1 - | |
| 2 - | 1S32 12:00 King's Cross - Aberdeen, to Edinburgh. P.Ref |
| 3 - | |
| 4 - | 1A22 11:00 Newcastle - King’s Cross. |
| s5 - | |
| 6 - | |
| 7 - | |
| 8 - | |
| 9 - | |
| 10 - | |
| 11 - | |
| s12 - | 1L16 13:20 King’s Cross - Bradford. |
| 13 - | |
| 14 - | |
| 15 - | Casualty report card states: loss of main
air - metal showing under overcharge valve (M8A valve changed). 40,000 miles since last classified repair (26.07.69). |
| 16 - | |
| 17 - | To Doncaster Works - Unclassified repairs. Repairs were carried out to interior lighting cables. Released from Doncaster Works. |
| 18 - | |
| s19 - | |
| 20 - | |
| 21 - | |
| 22 - | |
| 23 - | |
| 24 - | |
| 25 - | 1A12 08:10 Newcastle - King's Cross. |
| s26 - | |
| 27 - | |
| 28 - | 1S35 14:00 King's Cross - Edinburgh. |
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| 30 - | |
| 31 - |
November
| 1 - | |
| s2 - | |
| 3 - | Finsbury Park TMD. Shopping proposal dated 11.12.69 suggest loco off 1500-1800 hrs exam. |
| 4 - | Casualty report card states: Fuel leaking
on No.2 engine - HP fuel pipe leaking (fuel pipe union tightened). 48,000 miles since last classified repair (26.07.69). |
| 5 - | |
| 6 - | |
| 7 - | Casualty report card states: Main
generators flashed over - no apparent cause. 49,900 miles since last classified repair (26.07.69). |
| 8 - | 1S35 14:00 King’s Cross - Edinburgh. |
| s9 - | |
| 10 - | Finsbury Park TMD. Boiler J2950 on test - results: satisfactory for service. |
| 11 - | Casualty report card states: Slight
flashover on generators - no apparent cause (two flashpoints renewed). 51,500 miles since last classified repair (26.07.69). |
| 12 - | |
| 13 - | |
| 14 - | |
| 15 - | |
| s16 - | |
| 17 - | |
| 18 - | 1A15 09:15 Newcastle - King’s Cross, "The Tees-Tyne Pullman". |
| 19 - | Casualty report states: Permanent
wheelslip light - to be investigated (loco waiting 'Brush' regeneration). 54,000 miles since last classified repair (26.07.69). |
| 20 - | |
| 21 - | 1L03 07:45 King's Cross - Bradford. 1A21 11:55 Bradford - King's Cross. |
| 22 - | Casualty report card states: Earth fault on
boiler - resistance cover touching 'illegible' (resistance cover repositioned). 55,000 miles since last classified repair (26.07.69). |
| s23 - | |
| 24 - | |
| 25 - | |
| 26 - | |
| 27 - | |
| 28 - | 1A15 09:15 Newcastle - King's Cross, "The Tees-Tyne
Pullman". Finsbury Park TMD. Proposal for tyre turning: No.5 tyre has fairly large hole in tread left side. |
| 29 - | |
| s30 - | Casualty report card states: Continuous
wheelslip indication - detection equipment giving false indication (experimental equipment removed). 58,000 miles since last classified repair (26.07.69). |
December
| 1 - | |
| 2 - | |
| 3 - | Doncaster TMD. Tyre turning. |
| 4 - | To Doncaster Works - Unclassified repair. No.2 bogie 9000-4 No.4 axle suspension tube bearings seized and retaining plate set screws sheared - No.4 wheelset and traction motor were changed. |
| 5 - | Doncaster Works. |
| 6 - | Released from Doncaster Works. |
| s7 - | Casualty report card states: Slight
flashover on generators - no apparent cause (flashover damage cleaned up). 58,000 miles since last classified repair (26.07.69). |
| 8 - | |
| 9 - | Finsbury Park TMD. Shopping proposal dated 11.12.69 suggest loco off 500-600 hrs exam. |
| 10 - | Casualty report card states: Cab heaters
defective - wire broken on heater. 63,000 miles since last classified repair (26.07.69). |
| 11 - | Finsbury Park TMD. Taken out of traffic - awaiting works attention. |
| 12 - | |
| 13 - | To Doncaster Works - Unclassified repair. Shopping proposal states: Burnt cabling, suspect cable damaged in bodyside trunking and repeated trouble with heaters and lights not working - burnt wiring in control cubicles in both cabs and all necessary wiring in trunking repaired. A.V.R.'s and traction motor blower motors were checked. 60,000 miles since last classified repair (26.07.69). |
| s14 - | Doncaster Works. |
| 15 - | Doncaster Works. |
| 16 - | Doncaster Works. |
| 17 - | Doncaster Works. |
| 18 - | Released from Doncaster Works. |
| 19 - | |
| 20 - | Casualty report card states: Boiler would
not fire - electrode gap too excessive. 67,000 miles since last classified repair (26.07.69). |
| s21 - | |
| 22 - | |
| 23 - | 1A21 11:55 Bradford - King’s Cross. |
| 24 - | 1L03 07:45 King's Cross - Bradford. 1A21 11:55 Bradford - King's Cross. |
| 25 - | |
| 26 - | |
| 27 - | 1S32 12:00 King's Cross - Aberdeen, to Edinburgh. |
| s28 - | |
| 29 - | |
| 30 - | |
| 31 - |
D9001
(1968).....D9001 (1970)
1969.....HOME