D9015 - 1968
January
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| s7 - | 1E67 10:20 Bradford - King's Cross. |
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| 24 - | To Doncaster Works - General repair. Water scoop mechanism inoperative - power units No.1 457 replaced by 426 & No.2 440 replaced by 450, bogies No.1 9000-19 & No.2 9000-20 were given General repairs and boiler 1486/J2942 replaced by 5096/J3247. The water scoop mechanism was renewed, the body given a General repair and the locomotive fitted for dual braking. Power
unit 440 was officially credited as fitted: |
| 25 - | Doncaster Works. |
| 26 - | Doncaster Works. |
| 27 - | Doncaster Works. |
| s28 - | Doncaster Works. |
| 29 - | Doncaster Works. |
| 30 - | Doncaster Works. |
| 31 - | Doncaster Works. |
February
| 1 - | Doncaster Works. |
| 2 - | Doncaster Works. |
| 3 - | Doncaster Works. |
| s4 - | Doncaster Works. |
| 5 - | Doncaster Works. |
| 6 - | Doncaster Works. |
| 7 - | Doncaster Works. |
| 8 - | Doncaster Works. |
| 9 - | Doncaster Works. |
| 10 - | Doncaster Works. |
| s11 - | Doncaster Works. |
| 12 - | Doncaster Works. |
| 13 - | Doncaster Works. |
| 14 - | Doncaster Works. |
| 15 - | Doncaster Works. |
| 16 - | Doncaster Works. |
| 17 - | Doncaster Works. |
| s18 - | Doncaster Works. |
| 19 - | Doncaster Works. |
| 20 - | Doncaster Works. |
| 21 - | Doncaster Works. |
| 22 - | Released from Doncaster Works. Finsbury Park TMD. Casualty report card states: oil pressure flexible pipe burst - small gash in pipe (new pipe fitted). 450 miles since last classified repair (22.02.68). |
| 23 - | Doncaster TMD. Casualty report card states: No.1 engine cutting out - locomotive taken out of traffic. 1,025 miles since last classified repair (22.02.68). |
| 24 - | Doncaster TMD. |
| s25 - | Doncaster TMD. |
| 26 - | Doncaster TMD. |
| 27 - | To Doncaster Works - Unclassified repair. No.1 power unit 426 continually shutting down and No.1 main generator smoke coming from armature internally - the engine shutdown fault was rectified and the main generator was cleaned. |
| 28 - | Doncaster Works. |
| 29 - | Doncaster Works. |
March
| 1 - | Released from Doncaster Works. |
| 2 - | Finsbury Park TMD. Casualty report card states: boiler defective - water pump shaft drive sheared (new water pump fitted). 4,500 miles since last classified repair (22.02.68). 1A36 14:00 King's Cross - Edinburgh, "The Heart of Midlothian". |
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| 11 - | 1A73 19:15 Aberdeen - King's Cross, from Edinburgh. |
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| 22 - | 1A50 18:00 King's Cross - Newcastle, "The North Eastern". |
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| s24 - | |
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| 27 - | Casualty report card states: loss of power
- no fault found. 18,500 miles since last classified repair (22.02.68). |
| 28 - | Casualty report card states: No.2 exhauster
defect - brushes not seated correctly on commutator
(brushes renewed). 18,500 miles since last classified repair (22.02.68). |
| 29 - | |
| 30 - | Finsbury Park TMD. |
| s31 - |
April
| 1 - | |
| 2 - | |
| 3 - | |
| 4 - | Finsbury Park TMD. Casualty report card states: No.2 blower motor fuse blown - incorrect fuse fitted (correct fuse fitted). 19,500 miles since last classified repair (22.02.68). 1A60 19:40 King's Cross - Aberdeen, "The Aberdonian" to Edinburgh. |
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| s7 - | 1E67 10:20 Bradford - King's Cross. |
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| 12 - | 1A37 11:00 Edinburgh - King’s Cross (Sunday service). |
| 13 - | 1A23 10:00 Edinburgh - King's Cross, "The Flying Scotsman". |
| s14 - | |
| 15 - | 1A16 10:00 King's Cross - Edinburgh, "The Flying Scotsman". |
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| 26 - | 1N20 15:55 King's Cross - Harrogate. |
| 27 - | 1A36 14:00 King's Cross - Edinburgh, "The Heart of Midlothian". |
| s28 - | |
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May
| 1 - | |
| 2 - | Casualty report card states: boiler
defective - bad connection on HT leads
(connection remade). 33,000 miles since last classified repair (22.02.68). |
| 3 - | |
| 4 - | 1A23 10:00 Edinburgh - King's Cross, "The Flying Scotsman". 1A50 18:15 King's Cross - Newcastle. |
| s5 - | |
| 6 - | New timetable period (first to run 12 months consecutively) |
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| 10 - | To Doncaster Works - Unclassified repair. No.2 exhauster defective and running at excessive RPM - the defects were rectified and the speedometer was adjusted. Released from Doncaster Works. 1E87 17:40 Hull - King's Cross, from Doncaster. |
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| s12 - | |
| 13 - | 1N20 15:55 King's Cross - Harrogate, to Leeds. |
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| 17 - | To Doncaster Works - Unclassified repair. No.2 power unit 450 liner seal leaking - 450 replaced by 412 and an exhauster was replaced due to a motor defect. |
| 18 - | Doncaster Works. |
| s19 - | Doncaster Works. |
| 20 - | Doncaster Works. |
| 21 - | Doncaster Works. |
| 22 - | Released from Doncaster Works. |
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| 24 - | |
| 25 - | 1A36 14:00 King's Cross - Edinburgh. |
| s26 - | 1N14 12:20 King's Cross - Bradford. (3E91 17:50 Bradford - Grantham). |
| 27 - | (5B04) Grantham - Lincoln (ECS). 1B04 07:25 Lincoln - King's Cross. |
| 28 - | 1B04 07:25 Lincoln - King's Cross. |
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June
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| 5 - | 1E73 11:55 Bradford - King's Cross. |
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| s9 - | |
| 10 - | Casualty report card states: loss of lub
oil - pipe chafing on clip (pipe
renewed). 52,000 miles since last classified repair (22.02.68). |
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| s16 - | 1N16 13:20 King's Cross - Bradford. |
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| s30 - |
July
| 1 - | Casualty report card states: high water
temperature - unable to fault. 64,000 miles since last classified repair (22.02.68). |
| 2 - | |
| 3 - | |
| 4 - | 1E59 09:00 Bradford - King's Cross, from
Leeds.
PIC King's Cross Loco. 1N24 17:35 King's Cross - Harrogate, "The Yorkshire Pullman". PIC |
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| 18 - | 1A16 10:00 King's Cross - Edinburgh, "The Flying Scotsman". |
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| 23 - | Casualty report card states: No.2 engine
cutting out - sump pressurising (locomotive taken out of traffic). 76,000 miles since last classified repair (22.02.68). |
| 24 - | |
| 25 - | To Doncaster Works - Unclassified repair. No.2 power unit 412 cylinder head liner seal defective - 412 replaced by 436 and No.2 end lubricating oil tank and radiator were cleaned. Released from Doncaster Works. |
| 26 - | Doncaster TMD. Tyre turning. 1E87 17:40 Hull - King's Cross, from Doncaster. |
| 27 - | 1A37 10:30 Aberdeen -King's Cross, from Edinburgh. |
| s28 - | Casualty report card states: no more than
17" vacuum - unknown fault (21" subsequently obtained). 78,400 miles since last classified repair (22.02.68). |
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August
| 1 - | |
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| 3 - | 1A25 10:10 Edinburgh - King's Cross. |
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| 6 - | 1E79 12:00 Newcastle - Colchester, to York. 1A27 13:00 Newcastle - King's Cross, from York. King's Cross Loco. |
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| 15 - | 1A21 11:00 Newcastle - King's Cross. |
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| 17 - | 1A23 10:00 Edinburgh - King's Cross, "The Flying Scotsman". |
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| 23 - | Casualty report card states: brake defect -
VA1 valve diaphragm punctured (diaphragm changed). 90,000 miles since last classified repair (22.02.68). |
| 24 - | |
| s25 - | Casualty report card states: unable to
cancel AWS - key in south end in up position (key replaced). 91,200 miles since last classified repair (22.02.68). |
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| 27 - | |
| 28 - | Casualty report card states: low oil
pressure - liner leakage water in sump (locomotive taken out of traffic). 92,000 miles since last classified repair (22.02.68). To Doncaster Works - Light repair. No.1 power unit 426 suspect liner seal - power units No.1 426 replaced by 454 & No.2 436 was given an Unclassified repair, bogies No.1 9000-19 replaced by 9000-35 & No.2 9000-20 replaced by 9000-36 and boiler 5096/J3247 was given an Unclassified repair. The body was given an Unclassified repair. |
| 29 - | Doncaster Works. |
| 30 - | Doncaster Works. |
| 31 - | Doncaster Works. |
September
| s1 - | Doncaster Works. |
| 2 - | Doncaster Works. |
| 3 - | Doncaster Works. |
| 4 - | Doncaster Works. |
| 5 - | Released from Doncaster Works. |
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| s8 - | |
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| 12 - | 1A29 10:05 Perth - Caledonian Road, "Anglo-Scottish Car Carrier". |
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| s15 - | |
| 16 - | 1A26 12:00 King's Cross - Aberdeen, to Edinburgh. |
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| 19 - | 1A37 10:30 Aberdeen - King's Cross, from Edinburgh. PIC |
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October
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| 5 - | Finsbury Park TMD. |
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| 19 - | Casualty report card states: No.1 engine
shut down - loss of coolant (clip renewed). 22,000 miles since last classified repair (05.09.68). |
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November
| 1 - | 1A08 08:00 King's Cross - Edinburgh. Haymarket TMD. 1A43 16:00 Edinburgh - King's Cross, "The Talisman". |
| 2 - | 1A37 10:30 Aberdeen - King's Cross, from Edinburgh. |
| s3 - | |
| 4 - | |
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| 7 - | Doncaster TMD. Casualty report card states: No.2 engine not firing - solenoid changed. 32,000 miles since last classified repair (05.09.68). |
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| 21 - | Casualty report card states: boiler
defective. 39,000 miles since last classified repair (05.09.68). |
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| s24 - | |
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| 27 - | Doncaster TMD. Tyre turning. |
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| 30 - |
December
| s1 - | 1A41 12:15 Edinburgh - King's Cross (via Backworth). |
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| 4 - | |
| 5 - | Casualty report card states:
defective heater pipe - damaged preventing
coupling up. 46,500 miles since last classified repair (05.09.68). |
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| s8 - | |
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| s15 - | Casualty report card states:
loco slipping - greasy state of rails. 52,000 miles since last classified repair (05.09.68). |
| 16 - | 1E67 09:50 Harrogate - King's Cross, "The Yorkshire Pullman". |
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| s22 - | |
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| 27 - | Casualty report card states:
defective motor blowers - 'O' BA nut in blower
motor contactors (nut removed & contactors cleaned). 56,000 miles since last classified repair (05.09.68). |
| 28 - | 1A11 08:50 Newcastle - King's Cross. King's Cross Loco. |
| s29 - | Casualty report card states:
one engine cutting out - low megger reading
(locomotive taken out of traffic). 58,000 miles since last classified repair (05.09.68). |
| 30 - | |
| 31 - | To Doncaster Works - Unclassified repair. Lubricating oil in blower ducting at No.1 end and No.3 traction motor megger reading 200k (motor soaked in oil) - all traction motors on No.1 bogie 9000-35 were replaced and repairs were carried out to No.2 exhauster oil pump. |
D9015
(1967).....D9015 (1969)
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