D9003 - 1969

D9003 (1968).....D9003 (1970)

January

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Deltic Diagrams

1 -  
2 -  
3 -  
4 -  
s5 -  
6 -  
7 - Casualty report card states: Boiler failed - no fault found.
79,200 miles since last classified repair (19.07.68)
.
8 -  
9 -  
10 - Finsbury Park TMD.
Locomotive proposed for tyre turning
.
11 -  
s12 -  
13 -  
14 -  
15 -  
16 -  
17 -  
18 - Doncaster TMD.
Tyre turning.
s19 - Doncaster TMD.
Tyre turning.
20 - Finsbury Park TMD.
Shopping proposal dated 23.01.69 states: loco off 500-600 hrs exam
.
21 - Casualty report card states: Boiler defective - water pump circuit breaker tripped. Circuit breakers reset.
87,200 miles since last classified repair (19.07.68)
.
22 - (Peterborough TMD).
Casualty report card states: No.2 engine shut down - piston through crankcase. Loco to works
.
87,200 miles since last classified repair (19.07.68)
.
23 - Peterborough TMD.
Locomotive taken out of traffic - awaiting works attention.
Shopping proposal states: No.2 engine piston through B crankcase (loco at New England)
.
Work on No.1 engine to works.
87,200 miles since last classified repair (19.07.68) (97,000 actually stated)
.
24 - To Doncaster Works - unclassified.
No.2 power unit 449 piston through crankcase on 'B' bank - 449 replaced by 428.
Released from Doncaster Works.
0B02 Doncaster - Finsbury Park.
Finsbury Park TMD.
25 - 1A33 15:15 Newcastle - King's Cross.
s26 - Casualty report card states: Loss of power - no fault found.
89,000 miles since last classified repair (19.07.68)
.
27 -  
28 -  
29 -  
30 -  
31 -  

February

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Deltic Diagrams

1 - 1A41 17:25 Newcastle - King's Cross.
s2 -  
3 -  
4 -  
5 -  
6 -  
7 - Finsbury Park TMD.
Boiler test - satisfactory for service
.
Locomotive taken out of traffic - awaiting works attention.
Shopping proposal states: No.2 engine has lub oil in coolant water - suspect liner defect
.
Work on No.1 engine to works
.
92,000 miles since last classified repair (19.07.68)
.
8 -  
s9 -  
10 - To Doncaster Works - Unclassified repair.
No.2 power unit 428 lubricating oil in coolant (suspect liner defect) - a sample of coolant was taken and coolant topped-up.
Released from Doncaster Works.
11 - Casualty report card states: Defective heater pipe - lugs bent. Pipe changed.
97,600 miles since last classified repair (19.07.68)
.
12 - 1A42 16:00 King's Cross - Edinburgh, "The Talisman".
13 -  
14 -  
15 -  
s16 - Casualty report card states: Short of coolant - apparent mis-management. tank filled & to traffic.
111,000 miles since last classified repair (19.07.68)
.
17 -  
18 -  
19 -  
20 -  
21 -  
22 -  
s23 - 1A22 11:00 King's Cross  Newcastle. PIC
24 - Loco proposed for classified repair.
25 - To Doncaster Works - General repair.
No shopping proposal - power units No.1 424 replaced by 405 & No.2 428 replaced by 447, bogies No.1 9000-43 replaced by 9000-41 & No.2 9000-44 replaced by 9000-42 and boiler 5094/J3245 replaced by 1496/J2952. The body was given a General repair.
26 - Doncaster Works.
27 - Doncaster Works.
28 - Doncaster Works.

March

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Deltic Diagrams

1 - Doncaster Works.
s2 - Doncaster Works.
3 - Doncaster Works.
4 - Doncaster Works.
5 - Doncaster Works.
6 - Doncaster Works.
7 - Doncaster Works.
8 - Doncaster Works.
s9 - Doncaster Works.
10 - Doncaster Works.
11 - Doncaster Works.
12 - Doncaster Works.
13 - Doncaster Works.
14 - Doncaster Works.
15 - Doncaster Works.
s16 - Doncaster Works.
17 - Doncaster Works.
18 - Doncaster Works.
19 - Doncaster Works.
20 - Doncaster Works.
21 - Doncaster Works.
22 - Doncaster Works.
s23 - Doncaster Works.
24 - Doncaster Works.
25 - Doncaster Works (4 bay Crimpsalls).
26 - Doncaster Works.
27 - Released from Doncaster Works.
28 - 1E75 (engine failure).
Casualty report card states: One engine cut out
.
380 miles since last classified repair (27.03.69)
.
29 -  
s30 - 1A50 17:45 King's Cross - Newcastle (engine failure).
Casualty report card states: No.5 traction motor overheating - loco taken out of traffic
.
1,100 miles since last classified repair (27.03.69)
.
31 - Finsbury Park TMD.
Off 1500-1800hrs exam
.
Locomotive taken out of traffic - awaiting works attention
.
Shopping proposal states: No.5 traction motor armature overheated and thrown solder. Armature open circuit.
Can work train with No.2 & 5 traction motors isolated at track speed (reports of No.1 engine shutting down)
.
320 miles since last classified repair (27.03.69) - see previous casualty report
.

April

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Deltic Diagrams

1 - To Doncaster Works - Rectification.
No.1 power unit 405 cutting out, No.5 traction motor armature overheated, throwing solder and armature open circuit - the overspeed trip mechanism on 405 was replaced, all traction motors on No.2 bogie 9000-42 were examined (no fault was found).
2 - Released from Doncaster Works.
3 - Finsbury Park TMD.
Locomotive taken out of traffic - awaiting works attention
.
Shopping proposal states: No.4 traction motor armature burnt out & slight flash over on No.s 1,2,3 & 5 traction motors
.
Loco to shops with No.s 3 & 4 traction motors isolated. A defective gearbox from D9009 and header tank from D9011 were also returned to works in rear cab of 9003
.
640 miles since last classified repair (27.03.69) - see casualty report
...
Casualty report card states: Flashover & wheelslip - No.4 traction motor burnt out. Loco taken out of traffic
.
3,500 miles since last classified repair (27.03.69)
.
4 - Good Friday - Sunday service only.
(Finsbury Park TMD).
5 - (Finsbury Park TMD).
s6 - (Finsbury Park TMD).
7 - (Finsbury Park TMD).
8 - To Doncaster Works - Rectification.
No.1 bogie 9000-41 all traction motors light flashover damage & No.2 bogie 9000-42 No.4 traction motor burnt out and light damage toNo.5 traction motor - bogies No.1 9000-41 replaced by 9000-43 & No.2 9000-42 replaced by 9000-44.
9 - Doncaster Works.
10 - Released from Doncaster Works.
xxxx Doncaster - Peterborough (test run).
xxxx Peterborough - Doncaster (test run)
.
11 - 1E73 11:55 Bradford - King's Cross, from Leeds.
12 - 1A14 09:00 King's Cross - Newcastle.
s13 - 1A22 11:00 King's Cross - Newcastle.
14 -  
15 -  
16 - Casualty report card states: Reported loss of air
10,000 miles since last classified repair (27.03.69)
.
17 -  
18 - 1A36 14:00 King's Cross - Edinburgh.
19 -  
s20 -  
21 -  
22 -  
23 -  
24 -  
25 -  
26 -  
s27 -  
28 -  
29 -  
30 - Casualty report card states: Reported defective brakes - no fault found. DSD isolated.
18,500 miles since last classified repair (27.03.69)
.

May

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Deltic Diagrams

1 -  
2 -  
3 -  
s4 -  
5 - New timetable period
6 -  
7 -  
8 - 1N10 11:00 King's Cross - Newcastle.
9 -  
10 -  
s11 -  
12 -  
13 -  
14 -  
15 -  
16 - Casualty report card states: Reported DSD defective - no fault found.
26,500 miles since last classified repair (27.03.69)
.
17 -  
s18 -  
19 -  
20 -  
21 -  
22 -  
23 -  
24 - 1L33 17:05 King's Cross - Bradford.
s25 -  
26 -  
27 -  
28 -  
29 - 1S32 12:00 King's Cross - Aberdeen, to Edinburgh.
30 -  
31 -  

June

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Deltic Diagrams

s1 -  
2 -  
3 -  
4 -  
5 -  
6 - Casualty report card states: Water scoop not working.
28,500 miles since last classified repair (27.03.69)
.
7 - 1A33 17:20 Bradford - King's Cross.
s8 -  
9 -  
10 -  
11 - 1L22 15:55 King's Cross - Harrogate, to Leeds.
12 - 1S35 14:00 King's Cross - Edinburgh, to Darlington (engine failure).
Casualty report card states: Flat batteries - no fault found
31,500 miles since last classified repair (27.03.69)
.
13 -  
14 -  
s15 -  
16 - Finsbury Park TMD.
Shopping proposal dated 18.08.69 states: loco off 500-600 hrs exam
.
17 -  
18 -  
19 -  
20 -  
21 - Casualty report card states: Loss of main air pressure - No.1 end outlet pipe fractured. Air pipe welded.
36,000 miles since last classified repair (27.03.69)
.
s22 -  
23 -  
24 -  
25 -  
26 -  
27 -  
28 -  
s29 -  
30 - Casualty report card states: Brake defective - DSD isolated. No fault found.
42,000 miles since last classified repair (27.03.69)
.

July

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Deltic Diagrams

1 -  
2 -  
3 -  
4 -  
5 -  
s6 -  
7 -  
8 - Casualty report card states: Boiler defect - water pump cock fractured. New cock fitted.
43,000 miles since last classified repair (27.03.69)
.
9 -  
10 -  
11 -  
12 -  
s13 -  
14 -  
15 -  
16 -  
17 -  
18 -  
19 -  
s20 -  
21 -  
22 -  
23 - Finsbury Park TMD.
'C' exam & Boiler test - satisfactory for service
.
24 - Finsbury Park TMD.
'C' exam.
25 - Finsbury Park TMD.
'C' exam.
26 - Finsbury Park TMD.
'C' exam.
s27 - Finsbury Park TMD.
Shopping proposal dated 18.08.69 states: loco off 1500-1800 hrs exam
.
28 -  
29 -  
30 -  
31 -  

August

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Deltic Diagrams

1 -  
2 -  
s3 -  
4 -  
5 -  
6 - 1S17 10:00 King's Cross - Edinburgh, "The Flying Scotsman".
7 -  
8 -  
9 - Casualty report card states: Boiler defect - Water scoop not working - new mouthpiece fitted.
54,000 miles since last classified repair (27.03.69)
.
s10 -  
11 -  
12 - 1A35 17:00 Newcastle - King's Cross.
13 -  
14 - Casualty report card states: Boiler defect - Wheelslip light bulb above 60 mph - No.1 traction motor contacts badly burnt. Contacts cleaned.
50,000 miles since last classified repair (27.03.69) - 60,000 stated
.
15 -  
16 -  
s17 -  
18 - Finsbury Park TMD.
Locomotive taken out of traffic - awaiting works attention
.
Shopping proposal states: No.2 traction motor armature pinion adrift. No.5 traction motor contactor overload to check
. All traction motors slightly flashed over - 40mph light engine to works.
57,330 miles since last classified repair (27.03.69)
.
19 - To Doncaster Works - Unclassified repair.
No.1 bogie 9000-43 No.2 traction motor armature pinion adrift (suspect key sheared) and all traction motors slight flashover damage, No.2 bogie 9000-44 No.5 traction motor contactor overload and all traction motors slight flashover damage - No.s 2, 5 & 6 traction motors were replaced and all others cleaned up.
20 - Released from Doncaster Works.
21 - Doncaster TMD.
Locomotive taken out of traffic - awaiting works attention.
Shopping proposal states: AWS defective & all traction motors flashed over
.
Casualty report card states: Wheelslip relays flashed over.
57,000 miles since last classified repair (27.03.69)
.
22 - To Doncaster Works - Rectification.
All traction motors flashed over and AWS defective - No.1 & No.2 main generators had all brush boxes and commutator cleaned of flashover damage, all traction motors had flashover damage cleaned up.
23 - Released from Doncaster Works.
s24 - Casualty report card states: Flashover at 90 mph - No.2 main generator flashed over
58,000 miles since last classified repair (27.03.69)
.
25 -  
26 - To Doncaster Works - Unclassified repair.
No.1 main generator slight flashover damage, No.2 main generator severe flashover damage and one insulation pot to change, No.1 bogie 9000-43 No.3 traction motor brush box cable disconnected, No.2 bogie 9000-44 No.5 traction motor flashover - No.1 main generator was replaced, flashover damage on No.2 main generator was repaired and insulators and brush boxes were changed. Flashover damage on traction motors was repaired.
27 - Doncaster Works.
28 - Doncaster Works.
29 - Doncaster Works.
30 - Doncaster Works.
s31 - Doncaster Works.

September

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Deltic Diagrams

1 - Doncaster Works.
2 - Released from Doncaster Works.
3 -  
4 -  
5 -  
6 -  
s7 -  
8 -  
9 -  
10 -  
11 -  
12 -  
13 - 1E17 10:30 Aberdeen - King's Cross, from Edinburgh.
s14 -  
15 - Casualty report card states: No.2 engine cutting out - not determined. Loco still defective.
60,000 miles since last classified repair (27.03.69)
.
16 -  
17 -  
18 -  
19 -  
20 -  
s21 -  
22 - 1L33 17:05 King's Cross - Bradford, to Leeds.
23 -  
24 - 1L33 17:05 King's Cross - Bradford.
25 -  
26 - 1A03 07:00 Bradford - King's Cross.
1S32 12:00 King's Cross - Aberdeen, to Edinburgh. 
27 -  
s28 -  
29 -  
30 - Casualty report card states: Reported as short of boiler water - gauge showing empty. Tank filled.
61,000 miles since last classified repair (27.03.69)
.
1A09 08:40 York - King's Cross.

October

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Deltic Diagrams

1 -  
2 -  
3 - 1A22 11:00 Newcastle -King's Cross.
4 - 1S35 14:00 King's Cross - Edinburgh.
s5 -  
6 - Casualty report card states: Engines shut down - BCC tips burnt. BCC tips renewed.
48,000 miles since last classified repair (27.03.69) - obviously incorrect!
7 -  
8 -  
9 -  
10 -  
11 -  
s12 -  
13 -  
14 -  
15 -  
16 -  
17 -  
18 -  
s19 -  
20 -  
21 -  
22 - Casualty report card states: Loss of power - No.2 main generator in wrong position. Loco taken out of traffic (to Doncaster Works). Note: no recorded works entry.
61,800 miles since last classified repair (27.03.69)
.
23 -  
24 -  
25 -  
s26 -  
27 - Casualty report card states: Loss of power - No.2 engine shutting down - Metalastik drive sheared. Drive renewed.
63,000 miles since last classified repair (27.03.69)
.
28 -  
29 -  
30 -  
31 -  

November

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Deltic Diagrams

1 -  
s2 -  
3 -  
4 - Casualty report card states: Difficulties releasing brakes - DME Newcastle to circulate report.
63,000 miles since last classified repair (27.03.69) - as 27/10
.
5 -  
6 -  
7 -  
8 -  
s9 -  
10 -  
11 -  
12 -  
13 -  
14 - 1E11 12:00 Edinburgh - King's Cross.
15 - 1E05 10:00 Edinburgh - King's Cross, "The Flying Scotsman".
s16 -  
17 -  
18 -  
19 -  
20 -  
21 - 1A07 07:25 Newcastle - King's Cross.
1N25 17:00 King's Cross - Newcastle, "The Tees-Tyne Pullman"
22 - 1S17 10:00 King's Cross - Edinburgh, "The Flying Scotsman".
s23 -  
24 -  
25 -  
26 - 1S35 14:00 King's Cross - Edinburgh.
27 -  
28 -  
29 -  
s30 -  

December

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Deltic Diagrams

1 -  
2 - Loco proposed for classified repair.
1N06 07:55 King's Cross - Newcastle.
3 -  
4 -  
5 -  
6 -  
s7 -  
8 -  
9 - To Doncaster Works - Light repair.
Power units No.1 405 & No.2 447 were given Unclassified repairs, bogies No.1 9000-43 replaced by 9000-11 & No.2 9000-44 replaced by 9000-12 and boiler 1496/J2952 was given an Unclassified repair and water tank capacity modification was carried out.
10 - Doncaster Works.
11 - Doncaster Works.
12 - Doncaster Works.
13 - Doncaster Works.
s14 - Doncaster Works.
15 - Doncaster Works.
16 - Doncaster Works.
17 - Doncaster Works.
18 - Released from Doncaster Works.
19 -  
20 -  
s21 -  
22 -  
23 - Finsbury Park TMD.
Locomotive taken out of traffic - awaiting works attention
.
Shopping proposal states: No.2 main generator interpole at 10 o'clock position to frame
. Loco ok to run on one engine. No.2 cab heater circuit brakers removed for D9011.
4,000 miles since last classified repair (18.12.69)
.
To Doncaster Works - Rectification.
No.2 power unit 447 main generator defective - 447 replaced by 434.
24 - Doncaster Works.
25 - Doncaster Works.
26 - Doncaster Works.
27 - Doncaster Works.
s28 - Doncaster Works.
29 - Doncaster Works.
30 - Doncaster Works.
31 - Released from Doncaster Works.
1A11 08:55 Hull - King's Cross, from Doncaster (piloting D1660).

D9003 (1968).....D9003 (1970)
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