_________________ Major Component Files _________________

_________ Power Unit 413 _________



1782 - Photo: Paul Bettany.

Power unit 413 awaiting refitting to 55022 (D9000) "ROYAL SCOTS GREY" at Barrow Hill on the 11th September 2005...
 



1781 - Photo: unknown.

...The damage caused to P/U 413 on Friday 6th October 2006 when the unit put a 'leg-out-of-bed' whilst 55022 was powering the RTC "Autumn Highlander" rail-cruise...
 



1780 - Photo: unknown.

...Further damage shows the side of the power unit and the broken con rod, once attached to the piston head.
413's history table is seen below...
 

 

Locomotive:

Installation:
(No.1/2 End)

Off Works:
(Fitted)

On Works:
(Removed)

Fault/Reason For Removal:

Notes:

01

D9000

?

28/02/61

22/06/61

No details

Out VF

02

D9018

2

24/11/61

16/03/62

Pieces of pistons in chip tray

In VF/out RSH

03

D9001

2

03/09/62

01/04/63

Loco due classified repair

In DONC

04

D9013

1

11/04/63

23/09/63

Loco due classified repair

 

05

D9000

1

17/12/63

26/01/65

Loco due classified repair

 

06

D9019

1

05/03/65

13/05/65

No details

 

07

D9006

2

05/10/65

13/03/67

Loco due classified repair

 

08

D9008

2

01/07/67

16/04/68

Loco due classified repair

 

09

D9017

2

08/05/68

12/07/68

No details

 

10

D9006

1

08/11/68

03/06/69

Loco due classified repair

 

11

D9019

1

05/06/69

14/01/70

No details

 

12

9021

1

16/03/70

12/05/70

Loco due classified repair

 

13

9019

1

19/05/70

12/10/70

Main generator faults

 

14

9013

2

18/10/70

02/11/70

Suspect fractured liner

 

15

9003

2

24/01/71

16/03/71

Aerating

 

16

9001

1

05/08/71

27/03/72

Defective liner seal

 

17

9020

1

09/08/72

17/11/72

Fractured liner

 

18

9014

1

19/01/73

26/02/73

Loco due classified repair

 

19

9017

1

08/03/73

15/12/73

Loco due classified repair

 

20

55019

2

25/02/74

16/09/74

Dephased

 

21

55007

1

26/09/74

05/12/74

Aerating

 

22

55021

1

01/05/75

22/10/75

To allow 55005 back to traffic

 

23

55005

2

23/10/75

30/12/75

No details

 

24

55012

1

08/04/76

23/10/76

Breathing heavy

 

25

55020

2

16/11/76

25/04/77

Piston through crankcase

 

26

55013

2

05/10/77

13/12/77

Fractured liner

 

27

55010

1

11/01/78

06/07/78

Suspect fractured liner

 

28

55003

1

13/07/78

16/08/78

Primary shaft drive flange defective

 

29

55018

1

20/08/78

21/09/78

Scavenge blower drive broken

 

30

55015

1

19/10/78

29/01/79

Time expired

 

31

55019

2

02/09/79

10/04/80

Dephased

 

32

55022

2

14/05/80

01/08/80

Fractured liner

 

33

55012

1

23/09/80

13/04/81

Suspect dephased

 

34

55022

2

09/07/81

 20/01/07

Piston through crankcase

 

Installed in 17 locomotives: 00/01/03/05/06/07/08/10/12/13/14/15/17/18/19/20/21
55022 withdrawn 02/01/82 & sold for preservation 09/83 – power unit stored

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